Since > has been long-time, the railroad system
when ?repairs the guest freight vehicle wheel, the use equipment
major part all is some heavy machine-tool plant in 890 ages
productions C8011B wheel lathe, this lathe has two tool rests, each
tool rest brings two coordinate axes (X axis and the Z axis), uses the
electronic imitating method gets a light from another light the wheel
to the wheel rim and the roller face carry on the processing, roller
face shape as if chart 1:  Chart 1 Because the electronic imitating processing method
precision is not high, therefore processes the wheel rim roller face
shape is worse. Moreover the engine bed movement control aspect
uses the old style relay electric circuit control, the electric
circuit complex, the failure rate is high, has brought the certain
difficulty to the service. Along with our country railroad
enterprise development, for adapts the railroad implementation to
raise fast and the development high speed train need, the wheel wheel
rim roller face manufacture precision and ?repairs the standard
more and more high, but original already by far could not satisfy the
precision request with the imitating method processing wheel, was
satisfies this request to this engine bed implementation numerical
control transformation to be most economical, the most effective
method. In the recent two years, various railroad car section
and the wheel shop carry on the numerical control transformation in
abundance to its original C8011B wheel lathe, we in use Simens's 802
series numerical controls system for this engine bed transformation
process in, successively has used Simens's 802S, 802C, the 802D
numerical control system, among, uses the 802D numerical control
system the equipment to transform the plan comparatively to have the
typical nature. When chooses the equipment the transformation plan, first
needs to consider is satisfies several requests which the
transformation must achieve: 1st, the tool rest X axis and the Z
axis control changes by originally the imitating control by the
digital axis controls. 2nd, controls original engine bed all
movements by the original relay electric circuit control changes the
PLC control. After 3rd, the cutting roller face shape satisfies
the precision request, the concurrent operation is as far as possible
simple. Above in order to satisfy the condition, we have selected
Simens's 802D numerical control system, this system is the digitized
numerical control system which the siemens promoted in recent years,
in its lathe version standard disposition brought a PP72/48 template,
was allowed to realize 72 inputs and 48 outputs PLC controls,
simultaneously actuated the module is a two axle power module, was
allowed to bring two linear axis and a main axle, in has set at the
velocity feedback and the displacement feedback sensor in the servo
electrical machinery may form a half closed-loop control system with
the main engine thus to be able together to achieve the very high
engine bed precision. Moreover the price is moderate, has the
very high natural price compared to, may the very good satisfied
equipment numerical control transformation request. Because the C8011B wheel lathe uses two tool rests gets a
light from another light the wheel to the about roller face also to
process about, therefore we used two set of 802D system separately to
control the tool rest movement. But engine bed all movements
control then completely control unit controls by left tool rest 802D
the system PLC. Left side the 802D system main hardware
disposition is: 1st, PCU main engine 1 2nd, entire function vertical keyboard 1 3rd, PP72/48 template 1 4th, 611UE actuation power source 5KW 1 5th, 611UE two axle closed-loop control unit 1 6th, 611UE two axle power module 1 7th, 1FK6 electrical machinery 3000RPM18NM 2 8th, outside meets 2500P/ to revolve encoder 1 9th, tie cable and PROFIBUS data bus certain About two sides systems hardware disposition is
same, uses a SIMODRIVE611UE two axle control module to control two
servo electrical machinery separately to actuate X axis tool rest and
the Z axis tool rest. Right flank the systematic PLC unit only
processes system itself the PLC instruction. But MCP (engine bed
control panel) then with the engine bed movement button kneading board
integrates in together self-restraint. In the hardware disposition, we selected beside standard
disposition outside to meet revolve the encoder, selected the reason
as follows: Because the numerical control transformation condition
limits, although we the original X axis and the Z axis lead screw
changed into the ball bearing lead screw, but the middle transmission
system still for the old transmission system, led X axis and in the Z
axis 滑台 transmission process in the servo electrical machinery, X
axis and Z axis transmission structure like chart 2 showed:  Chart 2 By on chart obviously, said regarding X axis,
because the gear drive progression are not many, the transmission gap
is not big, therefore may use the velocity feedback and the
displacement feedback which in the standard disposition use servo
electrical machinery sets, this time X axis 滑台 the movement
precision also can answer the purpose. But said regarding the Z
axis that, the transmission progression are many, moreover also has
two levels of bevel gears transmissions, therefore transmission gap
big increase, if we still used the servo electrical machinery end
displacement feedback, then the Z axis 滑台 the movement precision
could not obtain the safeguard. The solution method although has
very much, for instance the gearshift transmission perhaps installs
diffraction grating ruler and so on, on the Z axis guide rail but
because the condition limits with reason and so on price all is not
very good solution. Regarding this peculiar circumstance, in
order to solve this problem, finally we considered used outside the
one has met in the Z axis ball bearing lead screw end connection
revolves the encoder means, connection method like chart 3.  Chart 3 This time the Z axis displacement feedback signal
direct examination is the Z axis ball bearing lead screw end
displacement signal, but the electrical machinery and between the ball
bearing lead screw the gear drive transmission gap is all contained in
has shut in the endless chain, therefore the Z axis 滑台 movement
precision obtained the very big enhancement, has satisfied the
precision request. But in the 802D system actuation disposition, in the line
profile shaft control connection has not certainly looked like 802S or
the 802C system equally has a special encoder connection, it only has
two receives electrical machinery feedback signal X412 and the X411
connection. How this time Z axis does outside meet the encoder
the signal to be supposed to connect? On the 611UE two axle
closed-loop control unit, we saw has a X472 connection, this
connection is uses for to receive the main axle the encoder signal,
but certainly does not have in ours numerical control transformation
as usefully as the main axle control, therefore we was allowed to use
this connection after the revision system interior parameter to accept
the Z axis outside to meet the encoder feedback signal. After
outside will meet the encoder tie cable like chart 3 the connection,
we will only need to revise the 802D system interior in the system
data and the two axle power module actuation data outside, set at in
the Z axis servo electrical machinery the displacement feedback signal
shield to use meets the encoder the feedback signal to be allowed. This kind meets the encoder outside the ball bearing lead
screw end installment the method installment conveniently, increase
cost not many but use effect very good, therefore the natural price is
extremely higher than. Needs to pay attention only is in
installs in the debugging process to want the careful establishment
related engine bed data. Regarding original engine bed black-white control electric
circuit transformation, although the engine bed movement certainly is
not very many, but controls complex, between the movement security
lock are mutually more, therefore appears in the original electricity
cabinet electric circuit extremely complex, but completely changed
into after 802D the system PLC unit control, the external control
electric circuit obtained the enormous simplification. 802D in
the system standard disposition PP72/48 template can provide 72
entrance points and 48 outputs spots, the input output enough engine
bed use, does not need likely other some numerical controls system
such to have extra to increase a I/O input output module. In in the numerical control processing procedure
establishment, 802D uses is the numerical control system general G
code programming. Procedure succinct, in this engine bed
programming, because processes the roller face shape precision request
is higher, moreover also set the very high request to the operation
simple user, therefore we has specially considered this point in the
procedure establishment. Like chart 1 shows, because processes
turn uses to the time operator is the diameter survey, but in ordinary
circumstances we when lathe machining programming 进刀 is uses the
relative coordinates in X axis direction the way perhaps the
hypothesis engine bed work piece coordinates, adopts a zero
displacement the method to carry on the processing, but certainly is
not suitable in this engine bed. In order to simplify the
operation, we used Simens in the system R parameter to establish the
cutting quantity, in procedure after corresponding R parameter
programming, operator when processing only had the wheel which the
input had to process in the R parameter to the diameter value, then
the procedure could automatically trade figures out the cutting
quantity and carries on the cutting, enormous convenience operation. Moreover because turn is stricter after the about diameter
of wheel processing size request, after processing about turn 径差
cannot be bigger than 0.5mm. Therefore we initial established in
the R parameter to adjust the cutting datum to the knife parameter.
Changes when the cutter bar length or the numerical control
system reference point may extremely quickly facilitate the revision
datum, causes the wheel which the input the diameter value and
actually cuts to the diameter value to maintain completely
consistently. Also some point is when the cutting turn to, regarding
other numerical control systems, the Z axis direction usual operator
in the inside after the knife needs in the Z axis current coordinate
figure input parameter, but in the 802D numerical control system may
read takes the current coordinate figure the function to be allowed to
cause the operator not to use the data-in, we only must increase
"r0=$AA-IM after the processing procedure [ Z>", the system may
directly read in the current Z axis coordinate figure to R parameter
R0 in, such operator when operation on only needed to input each shaft
coupling to the diameter of wheel value which had to process to be
allowed directly to process, extremely simple was convenient. In in an equipment numerical control transformation
process, the electronmagetic interference phenomenon always is in
installs debugs in the scene frequently to puzzle debugs personnel's
very major problem, because uses the old equipment the workshop and
the location generally speaking working conditions quite bad,
强干?source many, moreover the electrical network voltage
undulation is bigger, the zero curve, the grounding quality are not
very high, therefore frequently bumps into the disturbance phenomenon
in the debugging process. For the interference elimination,
designs and debugs the personnel to be able not but to pay the extra
very many energy. Below for example we once used other systems
in to carry on the numerical control transformation in the wheel lathe
to encounter the situation: Usually the numerical control system
all works normally, every day but always has 12 times of numerical
controls systems suddenly anxiously to stop in the work, screen visual
display alarm is X axis encoder hardware breakdown, after on again the
electricity the engine bed restores normally, regarding this we start
to suspect is moves the encoder damage perhaps the line contact is not
good, but looked up the very long time, took very many measures all
not to be able to eliminate this phenomenon the production, the final
inspection result determination was the system has received the
workshop voltage instantaneous undulation disturbance, afterwards
could not but enter the terminal in the equipment power source to
install a voltage stabilizing transformer, And alone has
installed a quality very good grounding. Although finally has
solved the problem, but has wasted the very much time and the energy.
After has used Simens's 802D system, because this system has
adopted the current extremely popular use Profibus data bus each
function module connected communication way, therefore not only the
structure is simple, moreover the anti-jamming big increase, reduced
the numerical control equipment to have each kind of unclear breakdown
phenomenon possibility because of the electronmagetic interference. Has carried on the numerical control transformation in us
to the railroad system many units' C8011B wheel lathe after Simens's
802D numerical control system, after the transformation engine bed
performance reliable, the processing precision high, the operation
simple, the maintenance is convenient, therefore obtained user's
widespread approval and highly appraises. |