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Fuji PLC touches the screen on charactron sealing machine application
Origin: Input time: 07-05-20 23:42:16English version

The >1. introduction Shanghai Yongxin color television limited liability company is develops, the production colored monitor primarily industry, technology crowded knowledge-intensive state-owned major industry. Along with the charactron output enhancement, this company original production equipment has not been able to meet the production needs, needs to start immediately the new special purpose equipment. In newly goes into production in the equipment, the our company has undertaken the painter's brush sealing machine electricity control section development work.
2. control systems hardware selects the sealing machine is completes the color television packing nitrogen, the seal electromagnetism gun machine, is in the painter's brush production essential equipment. Entire wrap machinery for entire automated control. Because must simultaneously control 3 axes, the present small PLC single plane generally only can simultaneously output 2 groups channels to control 2 sets of servos, therefore must utilize between PLC the communication function, in this aspect Fuji PLC simple communication way, the human nature programming contact surface happen to can satisfy our request. Therefore we selected the Fuji UG20 series to touch the screen, in Fuji SPB series 2 PLC and 2 RS485 communication module, smoothly constituted to three sets of servo electrical machinery control system.
3. applications programming
In 3-1 control diagram position machine Fuji touches screen POD Fuji PLC SPB - 1 Fuji PLC SPB - 2 to be responsible to control the rifle stock the servo electrical machinery to be responsible to control the flame the servo electrical machinery to be responsible to control to the center servo electrical machinery
In 3-2 control system synopsis control system each part of functions distinction as follows: (1) through touches the screen to input function and so on craft parameter, off-line debugging, manual movement; (2) two PLC is responsible to control three servo electrical machinery the movement. On the position machine gives PLC according to the work succession output correspondence start signal, PLC controls each servo electrical machinery revolution, after correspondingly works the step to complete, the PLC feedback completes the signal to on position machine. 􀂾
Touches between the screen partial POD man-machine contact surface and SPB1 selects 1:1 communication method, the picture divides into the basic picture, the automatic picture, the simulation picture, the hypothesis picture, the manual picture, reports to the police the picture altogether six parts. Among: The basic picture mainly completes automatic picture and so on the between picture, simulation picture cut; Automatic picture mainly to system automatic movement when the system working procedure, various axes position, the running status as well as the breakdown code carry on the monitoring. The simulation picture mainly uses in the off-line debugging work, may simulate the instruction through the picture in pressed key and the indicating lamp which on the position machine sends out, demonstrated various servo the position condition, brings the convenience for the entire machine debugging. In the hypothesis picture carries on the establishment to in various servo axis movement work step position speed. The manual picture carries on the manual low-speed control facing various servo axis, mainly uses in to debug the servo. Reported to the police in the picture to record each kind of breakdown information which in the system movement occurred, like the servo reported to the police, the servo moves the ultra regulation, PLC reports to the police, information and so on main engine breakdown.
􀂾 PLC partial PLC main solution to servo control, because between between three exchanges servos movement control has the fast linkage, therefore to between POD, SPB1, the SPB2 data communication high speed, was safe, the reliable performance set a higher request. But Fuji PLC provides the communication function has completely satisfied this aspect request, moreover the connection method is simple, debugging convenience. Takes between SPB1 and the SPB2 data communication gives an example, we use CPU the link this intercom way. SPB1 and SPB2 respectively connect a RS-485 communication adapter, between the adapter segment way selects 485 communications methods. Connection diagram as follows: Each PLC may establish the biggest 32 characters the data to check the region to use in mutually to read takes. Here, we suppose the SPB1 communication pattern are CPU link, the station number suppose are 00, 共用?the site size supposes is 32 characters, the corresponding address is D1E00~D1E1F.
Supposes the SPB2 communication pattern is CPU link, the station number supposes is 01, 共用?the site size supposes is 32 characters, the corresponding address is D1E20~D1E3F. In exchanges in the servo operating control, because in the craft confidentially requests the servo electricity to carry on continuously, the multi- spots position high speed localization, the use increase type localization instruction appears is not very convenient. According to the former numerical control engine bed programming experience, we used in the PLC absolute value programming instruction to control the servo positioning, this caused each position relative zero point all is fixed. In movement so long as unceasingly changes absolute location value this variable to be able the extremely simple realization servo positioning control. 4. subtotals this set of productions unit at present already invested produces the nearly for 2 months, the movement stably is reliable. Specially the man-machine contact surface convenient operating mode receives the scene operator's high praise. We also feel, in the servo movement control, uses Fuji PLC and the Fuji man-machine contact surface is a good choice. Low end small Fuji PLC has 2 channels pulses output in particular, each channel output frequency reaches as high as 100KHz, but also has consummates Yi Yong the correspondence function, its natural price compared to has the very big competitive advantage in small PLC.
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